13-04-2014, 19:37
Problema risolto con un aggiornamento del EV1 sensor, e' stata appena rilasciata la versione 1.06.
The Pilot now uses the highest value of bus Speed from SOG or STW. - This will eliminate the pilot instability issues seen on some vessels that have a faulty or non-inserted STW paddle wheel Transducer.
For vessels without SOG or STW, Cruising Speed is now selectable in Pilot Vessel Settings when Cal Lock is turned off.
Heading errors caused by vessels undertaking a fast banked turn is now corrected. – Previously seen as poor overlay performance.
Nel caso decideste di aggiornare, e' necessario aggiornare preventivamente l'ACU.
Buon vento!
The Pilot now uses the highest value of bus Speed from SOG or STW. - This will eliminate the pilot instability issues seen on some vessels that have a faulty or non-inserted STW paddle wheel Transducer.
For vessels without SOG or STW, Cruising Speed is now selectable in Pilot Vessel Settings when Cal Lock is turned off.
Heading errors caused by vessels undertaking a fast banked turn is now corrected. – Previously seen as poor overlay performance.
Nel caso decideste di aggiornare, e' necessario aggiornare preventivamente l'ACU.
Buon vento!
